OFF THE STRAIGHT AND NARROW
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MUSSELBURGH - On January 1st, 1941, Class D11 4-4-0 No.6390 HOBBIE ELLIOTT on a freight train crashed into Musselburgh Station, demolishing the bookstall and killing the attendant. Part of the stationmaster's house above was also damaged. The bathroom collapsed and the bath lay on top of the wreckage. The force of the crash caused some of the wagons of the train and their contents to come together in concertina fashion, and then shoot into the air. A heap of wreckage amassed in this way reached a height of about 30 feet and penetrated the station roof, which was holed in two places. Girders holding the roof fell across the platform and lines.
The guard on the train involved said there would be 550 tons weight in both the wagons and the engine of the goods train. At 7.17 a.m. they got a clear signal to proceed to Newhailes. The first indication he had that anything was wrong was just past Newhailes signal cabin, when he felt the train on a branch line he did not know, and which he did not think the driver knew. He applied the handbrake in his van, but the train was skidding down a gradient, and his action had little effect. Shortly afterwards there was a terrific crash.
David Little Ramage, signalman, said when the engine passed his cabin on the branch line to Musselburgh he waved a red lamp and blew a whistle. He thought that the train was a runaway.
John Renton Hunter (43), the driver of the engine of the goods train, said he did not know the Musselburgh branch line. The Newhailes distant signal was in the clear position, but he could not see the home signal. When he felt the train lurch on to the branch line he applied his brakes. The engine skidded, and he released the brakes and sanded the rails. Then he reapplied the brakes. The weight of the train appeared to be too heavy for the engine.
A fitter later examined the wreckage of the engine and could find no fault with the brakes.
Although the picture shows a scene of complete devastation, the engine was not badly damaged, being returned to service and withdrawn in September 1958 as BR No.62683.